Why Reserve Is Fun
April 29th, 2008Today (well, yesterday now) was the first day of a 5 day reserve block. They gave me 10am regular reserve and then called me at 4:18pm to get the hangar as quick as I could to fly a reposition flight down to Columbia, SC. Now, when they call, I have 1:30 to get to the airplane, even if they say “hurry”. I used about 1:15 of it to pack, fight traffic and walk to the hanger through a light rain. The plan was for us to fly down to CAE and then double deadhead through Charlotte and back to Dayton, getting in around 11:39pm.
The FO was already out in the plane so I headed through the MX hangar and outside to where it was parked. A quick check of the logbook showed it had been flown to Dayton to have a parking brake issue fixed. Basically, some times (not always though) when the parking brake was released there was an error message shown for about 10 seconds. Other then that it was a good airplane.
I started in on my checklists and wouldn’t you know it, when I released the brake to check the anti skid system, the same error message appeared. So much for them fixing it. I called up MX Control (who were just a few hundred feet away inside the hangar and they sent some mechanics out who had us shut down the APU while they connected a tug and pushed us backside the hangar.
We headed over to the break room and waited. And waited. The TV was on Fox and we sat through Seinfeld, According to Jim and two Simpson’s episodes (so we sat for 2 hours). Bones was just starting when I headed in to the Operations Control Center to find out what was going on. They said it was almost fixed and gave me new paperwork. About 20 minutes later we were back in the plane (which they had tugged back out of the hangar) and ready to try again. This time I tested the parked brake first, and sure enough, it failed again.
MX Control just laughed at me when I told them what had happened. They said they would send the guys back out, and while we waited I started running some numbers. The flight down there was scheduled for 1 hour and 25 minutes. I had to add to that our taxi out time and our taxi in time (5 and 10 minutes) and then a 15 minute debrief period. We started the day at 10am (on reserve) which meant 14 hours of duty time would be midnight. However, because of the MX delay, they could push us to 15 hours. 10+15 = 1am. Working back from 1am, I came up with the fact that we needed to be off the ground, heading towards CAE no later then 11:05pm. Otherwise we couldn’t go.
Nobody had come out yet, and there was another plane parked next to us that was about to head down to Mississippi to get painted. There were two crews on board, one flying and the other deadheading as there were two planes to pick up down there. I talked to them for a few minutes before they were readying to go, and our plane was getting hooked up to a tug for the second time that evening. Back in the hangar I spoke with one of the mechanics and he said they were probably going to try to change a part out, and put it in another plane. If it failed in there they knew the part was the problem and then they could replace it. But they didn’t have that spare so they would either have to cannibalize it from another airplane while they waited for the part to put back into the cannibalized airframe, or just sit it out and wait for the spare to put directly into the broken airplane.
At that point we had about 1:15 before we needed to be off the ground. The mechanic didn’t think it was going to happen so we headed back into OCC and told them the bad news. The MX Control Supervisor was just about to release us and cancel the flight when one of the line mechanics called her and said they could probably swap the part out of a good airplane and have us ready to go by 10:45. So much for going home.
I started wondering if we could get the plane out to the runway in 20 minutes. I certainly wasn’t going to push things just to get off in time. The minutes ticked by while we sat and waited. Finally at about 10:50 they said it was done and we headed out to the hangar again. The plane was still inside but the tug was hooked up and as soon as we got on board they closed the door and started pulling us out of the hangar. I got the APU going and power on the plane at around 11pm. At that point I was pretty certain it wasn’t going to happen. I released the brake and there was no message, so at least they had fixed the problem. I started running checklists knowing we weren’t going anywhere, and when we finally go the MX logbook back at 11:02, I told the FO to relax because we were done.
I called OCC over the radio and let them know it wasn’t going to happen. There was just no way we could have set up the plane for flight, started the engines, taxied out and taken off in 2 minutes. I wasn’t willing to rush to even try to make it happen at that point.
So, we shut the plane off, headed back inside (for the third time), thanked the mechanics for their effort and then headed out.
Both the FO and I agreed that we really did want to get the plane down there, and even though we both knew there was no way it was going to happen when we still hadn’t gotten to the plane by 10:45.
The good thing for me was I realized I will not be pushed around, and I am going to take the conservative route.
We’ll see what tomorrow brings.