3 Years
July 27th, 2008Yesterday marked three years of employment for me at my current job. I suppose, with the exception of working for Arts & Entertainment while I was in college for 4 years, this is the longest I have been at one job. I didn’t come into this specific job with any planned timeline, which is probably a good thing, as many of the people who did left when they found their timeline didn’t match reality. I know this job is a stepping stone to another job (hopefully the one I’ll retire from, but in this day and age who knows if that is even possible) but as to how long that takes, I have no idea. So, here’s to another three years.
The day itself was actually pretty bad. About midway through my FO looked at me at one point and said we just need to accept it’s going to be one of those days, and just deal with it. It actually didn’t start off too badly. I had breakfast at IHOP (for the second time in a month) with another FO who was overnighting in Akron as well. We then showed at 12:30 to fly down to Charlotte and get our day going. I have in legs this trip and I despite Charlotte allowing us to keep our speed up (they normally slow us down FAR, FAR away from the airport) I managed to get the plane slowed and on the ground rather nicely. As we started taxiing in, I was planning my upcoming 1:20 minute break. And that’s when the good part of the day ended.
They held us on the ramp for about 30 minutes due to traffic over on the Express gates. Then, once we got to our gate, which didn’t have a jetway, we unloaded all but 2 passengers and then had to wait 35 minutes for the rampers to find a ramp to get the last two passengers off the plane as neither one could do steps. After 35 minutes both passengers agreed to try the stairs and (with a whole lot of help) were about to get down and into wheelchairs. Now, my 1:20 break was down to 35 minutes and we had to swap airplanes.
Fortunately our plane wasn’t in yet so I was able to grab some food before it rolled up. We loaded up and had the door closed on time despite the late inbound, but were stopped from pushing 3 times due to late bags showing up and the rampers throwing them on. That’s fine (I want my passengers to get to their destination WITH their bags) but it made us 15 minutes late. After that fiasco we headed east to Jacksonville, NC, where the FO managed to survive a slam dunk approach (ATC kept us very high and fast) and landed the plane. Another quick turn, with rain showers approaching the field, and we were heading back west towards Charlotte.
ATC once again allowed us to keep our speed up for much longer then normal, which put a small check mark in the “plus” column for the day and 39 minutes after taking off I managed a pretty landing on 23 in Charlotte. Our momentary good luck continued with a gate actually be available for us and a ramp crew meeting us at the gate. We shut down and due to being early realized we had about an hour and fifty minutes before we were due back out to Charleston, WV for the overnight.
Because the plane was going to be sitting for a while I’d requested that they hook up ground power and air conditioning carts. That way I could shut down the APU and save some fuel while the plane sat. I could have just shut down the plane anyways, but due to the heat, I didn’t want the plane to get hot just sitting there. Also, by plugging in a power cart all the electronics stay on and that way we don’t have to re setup everything when we got back to the plane.
Of course there was no power or air carts waiting, and even after I verbally told the rampers all I got was a smile nod and after 20 minutes of waiting I just shut down the plane anyways and figured it would cool off when we turned it back on before departure. Also adding to the problems was the fact that the FO had discovered that one of the brake wear indicators wasn’t visible which means that the brakes are worn out. I wrote that up and called maintenance and then headed inside to the crew room.
When I got back to the plane an hour later there was an maintenance truck just pulling up. I asked them what the deal was with the brake and they said they had to replace it and it would probably take an hour. My FO had been right. It was just one of those days.
In the end we were only 30 minutes late off the gate (and that was mostly because we were waiting on two last minute passengers) and we were able to take off of 18L which is a much shorter taxi. My FO touched down in Charleston only 27 minutes late, which considering the day we’d had wasn’t too bad. Of course the hotel van wasn’t there, but they showed up eventually and thus our day ended, 11 hours, 4 legs and 1400 miles after it started.
3 more years? Hell yeah.